baustin
Well-Known Member
I need a little help troubleshooting my low boost issue. I've been running my Goblin since early 2020 and only ran into a low boost situation once, either replacing or fiddling with the boost bypass valve fixed the problem at that point. Let me know if you see where my understanding is wrong but I'll describe how I found this system works so far.
One morning I had normal throttle/boost response and then the next drive I don't get anything above ~3.5psi at any throttle position in any gear. I've done a few steps of troubleshooting but so far things haven't been fixed though I know there is a workaround, I'm trying to not leave my setup with the workaround yet.
It's a fairly simply system, here's the diagram for when the boost control solenoid (item 3) is open and the bypass valve (technically the bypass valve actuator, item 1) is open:
Here's the diagram for when the boost control solenoid is closed and the bypass valve is closed:
The boost control solenoid receives voltage from the PCM with the 1st wire and the 2nd wire to the solenoid is the ground wire. 0V signal causes the solenoid to stay open, high voltage signal closes the solenoid fully. I'm not sure what triggers the partial % between 0 and 100, if it's just a decreased voltage or if it's pulsing.
As long as the solenoid is closed, the bypass valve stays closed and the butterfly valve inside the supercharger stays closed. When the you are building boost and the solenoid opens, the bypass valve opens and turns the internal butterfly valve.
Places that can fail or cause problems: PCM configuration, wire from the PCM to the solenoid, ground wire to the solenoid, boost control solenoid internally fails to respond to voltage, hose leakage at any of the 3 hoses (items 2 / 4 / 11 in the diagrams), bypass valve actuator stoppage, bypass valve actuator leakage, bypass valve stuck.
All 3 hoses appear in good condition, no cracking. 1 or both of the top side hoses were replaced 3 years ago from hoses that were cracking significantly. I'm not 100% sure the hard to see hose (item 4) going to the intake manifold is perfect but I don't expect this could even be the issue based on other details.
To test the bypass valve (item 7): Disconnect the bypass valve actuator and check if the linkage spins freely.
-This worked normally for mine, no difficulty moving.
To test the bypass valve actuator (item 1): Disconnect the attached hoses and remove from the supercharger, depress plunger, place finger over 1 port at a time, release plunger, the plunger should not return to normal until you release your finger. You should not be able to blow air into 1 port and it come out the 2nd port.
-The plunger moved freely and did not return to normal while a finger was plugging each port, this should mean the internal diaphragm around the spring is still air tight. I don't have a number on how strong this spring should be, it feels like it did 3 years ago when I fiddled with it.
To test the boost control solenoid: You should be able to blow air through from the silver port or from the plastic port when no voltage is applied. The internal solenoid can be tested with a 9V battery and some alligator clips. When 9V is applied, you should hear a click noise from the solenoid and should no longer be able to blow air through the silver port. When 9V is applied, you should still be able to blow through the plastic port but the air will come out the foam covered port only and no air from the silver port
-My boost control solenoid tested open for the air but failed to actuate or change with a 9V. I ordered a new one and it did actuate properly with 9V and all these test steps
My tune call for 100% boost control solenoid (BCS) once the engine is turned on, expect for when in first gear. First gear is limited to 85% per the typical Cobalt tune and in the Goblin I'm not sure I could make use of those few extra psi in 1st gear.
To test the wiring and verify the tune is trying to control the boost control solenoid as expected: Disconnect the wire plug for the boost control solenoid, turn the key to 'run' without starting the engine, use a multimeter for the voltage on the 2 wires.
-My voltage is a constant 10.59V sitting during idle, I'm not sure if 10.59 is a problem but since a 9V battery actuates the solenoid I expect this is within the normal operating range
Nothing has changed with my tune for a long time, it's set to limit to 85% boost in first gear and then 100% boost allowed in all other situations:
When I data logged what was happening when I started troubleshooting this was the result. 2nd set of graphs, bright green line is the boost value. BCS is graphed in the top data set and is correctly indicating it's calling for 85% during first gear though the flat line of boost shows that 85% and 100% has no impact currently. My stock boost gauge is showing exactly the same pressures that HPTuners is graphing.
What's next?
One morning I had normal throttle/boost response and then the next drive I don't get anything above ~3.5psi at any throttle position in any gear. I've done a few steps of troubleshooting but so far things haven't been fixed though I know there is a workaround, I'm trying to not leave my setup with the workaround yet.
It's a fairly simply system, here's the diagram for when the boost control solenoid (item 3) is open and the bypass valve (technically the bypass valve actuator, item 1) is open:
Here's the diagram for when the boost control solenoid is closed and the bypass valve is closed:
The boost control solenoid receives voltage from the PCM with the 1st wire and the 2nd wire to the solenoid is the ground wire. 0V signal causes the solenoid to stay open, high voltage signal closes the solenoid fully. I'm not sure what triggers the partial % between 0 and 100, if it's just a decreased voltage or if it's pulsing.
As long as the solenoid is closed, the bypass valve stays closed and the butterfly valve inside the supercharger stays closed. When the you are building boost and the solenoid opens, the bypass valve opens and turns the internal butterfly valve.
Places that can fail or cause problems: PCM configuration, wire from the PCM to the solenoid, ground wire to the solenoid, boost control solenoid internally fails to respond to voltage, hose leakage at any of the 3 hoses (items 2 / 4 / 11 in the diagrams), bypass valve actuator stoppage, bypass valve actuator leakage, bypass valve stuck.
All 3 hoses appear in good condition, no cracking. 1 or both of the top side hoses were replaced 3 years ago from hoses that were cracking significantly. I'm not 100% sure the hard to see hose (item 4) going to the intake manifold is perfect but I don't expect this could even be the issue based on other details.
To test the bypass valve (item 7): Disconnect the bypass valve actuator and check if the linkage spins freely.
-This worked normally for mine, no difficulty moving.
To test the bypass valve actuator (item 1): Disconnect the attached hoses and remove from the supercharger, depress plunger, place finger over 1 port at a time, release plunger, the plunger should not return to normal until you release your finger. You should not be able to blow air into 1 port and it come out the 2nd port.
-The plunger moved freely and did not return to normal while a finger was plugging each port, this should mean the internal diaphragm around the spring is still air tight. I don't have a number on how strong this spring should be, it feels like it did 3 years ago when I fiddled with it.
To test the boost control solenoid: You should be able to blow air through from the silver port or from the plastic port when no voltage is applied. The internal solenoid can be tested with a 9V battery and some alligator clips. When 9V is applied, you should hear a click noise from the solenoid and should no longer be able to blow air through the silver port. When 9V is applied, you should still be able to blow through the plastic port but the air will come out the foam covered port only and no air from the silver port
-My boost control solenoid tested open for the air but failed to actuate or change with a 9V. I ordered a new one and it did actuate properly with 9V and all these test steps
My tune call for 100% boost control solenoid (BCS) once the engine is turned on, expect for when in first gear. First gear is limited to 85% per the typical Cobalt tune and in the Goblin I'm not sure I could make use of those few extra psi in 1st gear.
To test the wiring and verify the tune is trying to control the boost control solenoid as expected: Disconnect the wire plug for the boost control solenoid, turn the key to 'run' without starting the engine, use a multimeter for the voltage on the 2 wires.
-My voltage is a constant 10.59V sitting during idle, I'm not sure if 10.59 is a problem but since a 9V battery actuates the solenoid I expect this is within the normal operating range
Nothing has changed with my tune for a long time, it's set to limit to 85% boost in first gear and then 100% boost allowed in all other situations:
When I data logged what was happening when I started troubleshooting this was the result. 2nd set of graphs, bright green line is the boost value. BCS is graphed in the top data set and is correctly indicating it's calling for 85% during first gear though the flat line of boost shows that 85% and 100% has no impact currently. My stock boost gauge is showing exactly the same pressures that HPTuners is graphing.
What's next?
- I installed my replacement boost control solenoid that passed the bench test and went for a drive. Exactly 0 difference, the boost was still limited to ~3.5-3.7psi.
- I then tried the manual override setup of disconnecting the hose from the boost control solenoid to the bypass valve actuator, keeping it attached to the boost control solenoid and plugging the empty end with a bolt (and I added some tape around the bolt to ensure it was pressure tight). This effectively removes the electronic control of the boost level. The next data log is the result, boost was fully back in action. Keep in mind I have 2.9" pulley, not the stock size.
- ZZP offers replacement bypass valves (~$130 before tax currently), it could be that the bypass valve I have passes my simple bench test but should be replaced.
- Given that I'm getting a constant 10.59V on multimeter, I don't think I have a PCM / wire / ground issue.
- The original boost control solenoid does fail my bench test and the new solenoid passes the bench test but the boost pressure behavior is identical.
- I can leave the hose plugged to defeat the entire boost control solenoid but this isn't my first preference but it would be better than not having any useful boost pressure.