- Corey Well-Known Member
Recap:
Took for 1/4 mile drive on 2/19/2023, Extreme power!!
Started Goblin on 2/20/2023 to back out of garage and clean garage, Started normally which means a couple of tries and blip the gas pedal and she started. Really 45 secs of run time at best.
Went to pull back in the garage after cleaning and would not start.
No consistent fuel at the schrader valve last night.
Spark at cylinder 1.
Update:
Schrader valve at the fuel line does appear to give consistent fuel now. Previously the valve only trickled but after disconnecting the fuel filter earlier the fuel started to flow as I would expect. FALSE HOPES AND DREAMS when the schrader acted normal.
Pulled spark plugs and all seemed slightly damp, sprayed with brake kleen and reinstalled. Had a couple blips of hope but that was all.
Sprayed some engine starter fluid in intake pipe between the A2W and manifold, nothing new.
Placed rag over intake pipe and could see suction was being developed while cranking. Placed rag in spark plug hole during cranking and could see rag trying to be pushed back up.
Drained oil and checked for metal shavings. No metal shavings found on magnet.
Inline fuel pressure gauge leaks down from 49 psi to 20 psi after around 10 mins.
Honestly I am starting to lean towards timing is slightly off due to blipping the throttle to start before yesterday and if it jumped a tooth during 2/19/2023 drive.
Took for 1/4 mile drive on 2/19/2023, Extreme power!!
Started Goblin on 2/20/2023 to back out of garage and clean garage, Started normally which means a couple of tries and blip the gas pedal and she started. Really 45 secs of run time at best.
Went to pull back in the garage after cleaning and would not start.
No consistent fuel at the schrader valve last night.
Spark at cylinder 1.
Update:
Schrader valve at the fuel line does appear to give consistent fuel now. Previously the valve only trickled but after disconnecting the fuel filter earlier the fuel started to flow as I would expect. FALSE HOPES AND DREAMS when the schrader acted normal.
Pulled spark plugs and all seemed slightly damp, sprayed with brake kleen and reinstalled. Had a couple blips of hope but that was all.
Sprayed some engine starter fluid in intake pipe between the A2W and manifold, nothing new.
Placed rag over intake pipe and could see suction was being developed while cranking. Placed rag in spark plug hole during cranking and could see rag trying to be pushed back up.
Drained oil and checked for metal shavings. No metal shavings found on magnet.
Inline fuel pressure gauge leaks down from 49 psi to 20 psi after around 10 mins.
Honestly I am starting to lean towards timing is slightly off due to blipping the throttle to start before yesterday and if it jumped a tooth during 2/19/2023 drive.